“The Old Girl” Rides Again
By
Alan Lane-Richardson
After
many years of continual use and abuse “The Old Girl”, my 1969 Moto Guzzi
V7 Special, needed some major attention. The electrics were a bit of a
mystery with wires stuck in any lug hole that could be found that could
feed power to the required object that needed electrons to make it go. The
motor rattled and clanked but still worked, and rust was taking over
causing the front mudguard and side covers to slowly disappear. So I
decided that what was needed was a headlight to taillight makeover.
I’d
already carried out some work on the bike including the gearbox and the
front suspension. The gear box repairs were rudimentary, lots of cash and
get the hands dirty, whereas the front suspension proved a bit trickier.
The suspension repairs started out as a simple job to fix a few bits and
“She’ll be right” by a mob who gave the job to an apprentice. On the first
ride out, it rained and I discovered that the work done wasn’t as expected
when the front end locked up almost chucking me of the bike. Zenith
Engineering (www.zenith.net.au)
and RAD (www.radhardchroming.com.au) were employed to rebuild the now totally
stuffed forks back to standard tolerances and fix the left hand fork boot.
Some 30,000+ kms later they are still in good order.
D Day
arrived around January 2005 when the bike was pulled apart in preparation
for a well overdue overhaul. How much of an overhaul was unknown even
though some items such as paintwork, brakes, and electrics were on the
agenda, and lots of important questions had to be answered (and asked)
along the way.
In
particular the condition of the motor was a shock. The motor still ran and didn’t
blow a lot of smoke even though oil leaked from just about everywhere. Once the motor was pulled apart we found
the front bearing for the motor was so badly worn that there were grooves
in the crank and you could physically rattle it by hand. In addition, the
valve guides were badly worn, the valves and valve seats were shot, and
one head was cracked. The piston rings were worn, rockers were worn, cam
thrust washer was worn, and the oil pump gears were also worn. Yes, the
motor was technically stuffed! What to do?
Don Newell Motorcycles (www.newellmotorcycles.com.au) provided most of the
parts for the motor and what couldn’t be found in Australia came from
Teo Lamers (www.tlm.nl). Zenith Engineering was also employed
to check and adjust tolerance for the cam, crank and oil pump once I had
completed the preliminary motor rebuild. The crank had been reground but
didn’t need rebalancing because, let’s face it, the bike is not for
racing. But not to skimp, a check of the con rods, and pistons was carried
out to ensure their weights were well within tolerance on Meredith’s
kitchen scales. With the necessary motor parts in hand, crank reground, heads refurbished,
rockers rebuilt, and motor tolerances checked I put the motor together by
March 2006.
What
colour scheme? What design? What logo? Painting the bike was one of my
biggest dilemmas. Being a Libran changing my mind is just part of the
game. Fortunately Mark from Queensland Motorcycle Panel and Paint
(www.qmpp.com.au)
didn’t completely lose it but instead sat me in his office with a fist
full of colour charts to gaze at. Some colour charts later and checking
out lots of cars and bikes I knew what colour scheme I wanted. The rest is
history and eventually the panels that were broken were rebuilt and the
bits that needed painting were painted by January 2006.
Do I
want stainless steel? Do I want chrome? Finding header pipes and mufflers
is not as easy as one might think especially when you want the same
materials throughout to original specifications. I could get stainless steel header pipes but no
stainless steel mufflers. I could get chromed mufflers but no chromed
header pipes. Muffler manufacturers in Australia wanted a fortune to
reconstruct what I had in chromed mild steel and refused point blank to
try and bend stainless steel header pipes to the original specifications.
Pipe manufacturers wanted to make dies for $500 and an order for some
absurd number of header pipes. Eventually after surfing the net and some
general chatting I found what I wanted. Teo Lamers provided the
header pipes in stainless steel for under $100 each landed in Australia,
and Peter H from Gympie, right here in good old Oz, provided some
absolutely immaculate hand made stainless steel mufflers and clamps manufactured to
original specifications for a reasonable price. The final fitting of the
exhaust system was in April 2006.
Did I
have everything? Once the basic bike and motor was back together it was
time to locate some of the other bits that were needed. Teo Lamers
was the perfect choice to find wiring looms that fit straight onto V7,
Ambassador, and Eldorado’s cheaper than I could make it myself. In
addition I was able to locate the two front mudguard brackets for
reasonable prices.
The
time had arrived to fit some tyres. What tyres to fit? How do you select a
tyre? The decision was made to find a tyre with a tread that was similar
to that of tyres from the 60’s era. Simple it sounds but not that simple
when you realise just how few manufacturers make such a tyre that fits an
18” wheel. A quick search on the net and it’s AVON to the rescue and a
trip down to Tyres For Bikes to check out availability and prices.
Tyres were purchased and fitted in March 2006.
How
do you stop? The original brake shoes were not completely worn. However,
the brakes could slow the bike down but they couldn’t stop the bike in a
fit. 30 years ago finding someone to fit shoes to brakes was probably an
easy thing. These days with disc brakes almost fitted to everything there
aren’t that many people around that want to go down the old brake shoe
road. Once again thanks to Internet technology and the good old yellow
pages phone book I found TBS right here in Queensland who would do
the job and at a good price. The new brake shoes are a softer compound and
the bike now stops as required. The brakes were refurbished in March 2006.
What
to sit on? Sore point this one. Most bikes have a seat of some kind. Mine
had one but still in bits stuck on some shelf in someone else’s shed. I
did get it back after riding there to say g’day sitting on a cushion. I
think the impetus of my visit prompted the quick response of one
sit-on-able seat but not much else. It was quite obvious a quick search of
the Internet was needed to locate a new seat. Harpers Moto Guzzi (www.harpermotoguzzi.com) in
the US provided an LAPD single seat with a matching luggage rack and
pillion pad. The single seat is very comfy and fitted without alteration -
which is a first. The seats and rack were fitted in June 2006.
What
condition are things in? Of course not everything else was clear sailing.
When dismantling the bike it was found that some threads were badly
damaged or worn and some fittings were badly damaged. As a bit of a side
issue Zenith Engineering manufactured the following items in
stainless steel to original specifications: front and rear engine bolts,
engine/frame spacers, front and rear axles, studs for the handle bar
clamps, skid bars for the motor sump, side stand and
centre stand spacers and bolts. These items were manufactured over the
rebuild period. In addition I machined and polished the heads of all
stainless steel bolts used on the bike, sort of give it that finished
shiny look.
Is
everything alright? Since the rebuild the bike has successfully completed
its first 3,000 kms with no issues other than a seal leaking around the
distributor and a crook generator. A quick trip to a bearing shop soon
located a new O ring to stop that dreaded oil seepage. Hamilton Auto
Electrics were employed to rebuild the generator and to refurbish the
regulator in May 2006 (just before ending up in hospital for an operation
that meant missing out on the Ruptured Budgie Rally).
How
on earth do you set things up? The final setup of the motor was carried
out using my eyes, ears and a H2O U tube. The timing was
achieved by setting the crank to 10o by calculating the degrees
per tooth on the flywheel. Once the crank is at 10o I used a
magnifying glass to detect the point gap just starting to open when
twisting the distributor. Don’t smoke so don’t have cigarette papers.
Tuning of the motor was done by running each cylinder as a big single to
set air mixture and initial idle speed. To synchronise the cylinders
and final idle speed I attached a U tube that hangs from the roof of the
shed. The U tube has about 2m of head. I can get the accuracy pretty close
to a couple of Pascal’s from idle up. Like any tune up, a trip up Mt
Glorious tests the timing and the clutch doesn’t slip. A good run out
round Esk tests the fuel economy and engine performance at high speed.
While around town tests the idle when sitting at the lights. The final setup
was carried out in June 2006 after an extended and comprehensive run in period.
Where
is the key ring? Of course a bike isn’t finished until you receive that
key ring for the key that sits in the ignition from your loved one.
Meredith slaved for hours making a bead key ring with the letters V7
embroidered. A simple thing? No! Bike trips to the gold coast and local
shops were made to gather a variety of beads in many colours and sizes.
Meredith painstakingly put together many key ring samples until the
perfect colour, size and lettering combination was found to keep me happy. Of course the
key ring has pride of place hanging off the ignition key sitting in the
ignition of the bike up front where I can look at it regularly.
The
bike runs well and is a real treat to own. How many hours did it take? How much
did it cost? Well, I actually can’t tell you because I don’t actually
know. How long is a piece of string? I will say you will need a decent
shed, a buff/polisher, plenty of spare time and plenty of patience before
starting this type of project.